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CamBam help (General usage) / Re: Machining Polycarbonate - Progress
« on: November 28, 2022, 00:24:42 am »
I did some test cuts and used those learnings to cut another polycarbonate lid.
Changes:
.25"D and .031"D End mills were polished O-flute.
I added spiral lead in moves to everything.
Everything was cut at 45 in/min except the logo which was 30 in/min
I used soapy water for the logo cut only chasing the cutter and clearing chips with a wet chip brush, everything else was cut dry.
I reduced DOC on the dish cuts to the filter gland so there was a light finish cut.
I reduced depth of cut on the .25D EM perimeter cuts to .1". I used a rouging cut at .35 width which was the longest of ops, then two full depth finish cuts removing .005" each time.
The stock was secured with six screws. The stock was warped .090" high in the middle over 21" of length.
The screws were able to pull it flat but not very happy with the stock flatness.
I removed the protective film for all machining.
General Impressions:
Significant improvement over previous attempt. Still some areas could be better. I uploaded a high(er) resolution photo.
The logo is crisp and I'm quite satisfied with how it cut.
The ornamental grooves are ok, had some minor burrs here and there on the surface edges that needed to be struck off with a razor, but a fair trade for me to be able to cut it dry.
The dish cut on the filter gland is much better......still some tool marks but much improved.
The perimeter cut is much better but still the most difficult for my machine and leaves greatest room for improvement.
I think I'm bumping into the limits of my machine rigidity greatly aggravated by my having the router fully extended and all things biased for maximum stroke and height under gantry. It's just a hobby machine fellas. It just makes for a lot of cantilever leverage on the Z-axis and the it's not exceptionally rigid to begin with, coupled with the fact that it rides on extruded aluminum gantry this 44" in both X & Y. I think I can stiffen it up a bit and have a few things on my upgrade list. I'm sure cutting these ops with fluid would help. I'm just not set up adequately to do so, but could remedy that.
I can do a little hand work on the perimeter and this one and it will be passable. I think I may order some acrylic and make a couple for comparison. I'll post some completion photos when I get there.
Best,
Kelly
Changes:
.25"D and .031"D End mills were polished O-flute.
I added spiral lead in moves to everything.
Everything was cut at 45 in/min except the logo which was 30 in/min
I used soapy water for the logo cut only chasing the cutter and clearing chips with a wet chip brush, everything else was cut dry.
I reduced DOC on the dish cuts to the filter gland so there was a light finish cut.
I reduced depth of cut on the .25D EM perimeter cuts to .1". I used a rouging cut at .35 width which was the longest of ops, then two full depth finish cuts removing .005" each time.
The stock was secured with six screws. The stock was warped .090" high in the middle over 21" of length.


I removed the protective film for all machining.
General Impressions:
Significant improvement over previous attempt. Still some areas could be better. I uploaded a high(er) resolution photo.
The logo is crisp and I'm quite satisfied with how it cut.
The ornamental grooves are ok, had some minor burrs here and there on the surface edges that needed to be struck off with a razor, but a fair trade for me to be able to cut it dry.
The dish cut on the filter gland is much better......still some tool marks but much improved.
The perimeter cut is much better but still the most difficult for my machine and leaves greatest room for improvement.
I think I'm bumping into the limits of my machine rigidity greatly aggravated by my having the router fully extended and all things biased for maximum stroke and height under gantry. It's just a hobby machine fellas. It just makes for a lot of cantilever leverage on the Z-axis and the it's not exceptionally rigid to begin with, coupled with the fact that it rides on extruded aluminum gantry this 44" in both X & Y. I think I can stiffen it up a bit and have a few things on my upgrade list. I'm sure cutting these ops with fluid would help. I'm just not set up adequately to do so, but could remedy that.
I can do a little hand work on the perimeter and this one and it will be passable. I think I may order some acrylic and make a couple for comparison. I'll post some completion photos when I get there.
Best,
Kelly