I was able to successfully cut the cover plate for my intake manifold today.
It wasn’t completely without incident. I learned a few things and have a couple new questions. During the course of machining the part, I had a chance to use the drilling MOP. I had the foresight to drill a few test holes and O-ring glands in the waste area of the stock to test feeds and speeds and do some fine tuning to accommodate my machine. I was using a .125” 2 flute spiral carbide end mill. After doing so, the .199” holes were being cut ~.008” under size. That had me scratching my head. I moved on and cut a round O-ring gland with a .25” end mill and it cut correctly. I thought I was going to be coming back here and asking for help on that one and then, I thought to measure the 1/8" end mill……it checked .118”!………somewhere along the line I was sold a 3mm end mill and it should not have happened from the source it came from!
Anyway, I corrected that and got on with it. On the first few test cuts I could tell I was going to need cutting fluid because the cutter was already loading a little with aluminum. The stock was .25” thick ground MIC6 aluminum plate. It’s 7000 series but it is cast. So I manually used a squirt bottle to dispense fluid in front of the cutter as it was cutting. Once some slot depth got established it was easy because it collected the fluid and all I had to do was use the nose of the squirt bottle to drag the chips out of the groove after it was cut. Feedrate was slow so that was easy to keep up with.
The O-ring grooves were .121” wide and .082" deep being cut with a .094 HSS TiNC coated EM. All went well until the first lap of the perimeter O-ring groove. Halfway around the first cut, which was the last operation on the whole part, the end mill tip failed and was obvious from the sound and appearance of cut. The cutter now looked like a point cutting email. Must have gummed up despite my makeshift efforts to lube it. I paused, and the damage was not going to clean up at the present gland size so to save the piece, I decided to increase the O-ring gland size from 3/32” to 1/8” cross section O-ring, and resumed cutting.
It'd probably never make the grade for you guys but it should work fine for me. Pictures attached.
So, the question: After discovering my problem with drilling was the wrong PP, I selected the correct one. In the Tools menu, I have selected “settings saved on exit”. When I went to run the program (using grbl machine plug in), I looked at the PP and it had changed from Grbl1Millrite to Grbl Machine. When I reopened the file just now, it’s back to “default” PP. I didn’t consciously change anything.
How do I save the settings, like the PP, the out file name/extension, number format, etc? I thought that>Tools> “settings saved on exit” would do it but apparently not. Do I need to make a template or other?
Thanks for the help fellas.
Best,
Kelly